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Maximising AFR in Cement Manufacturing

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Shreesh A Khadilkar, Consultant and Advisor, and Former Director Quality and Product Development, ACC Ltd Thane, discusses the importance of optimising the use of alternative fuel and raw materials (TSR percentage) in cement production without affecting clinker quality.

We all know that in the calciner the CaCO3 undergoes calcination producing CaO, part of this CaO reacts with Al2O3, Fe2O3 SiO2 to form aluminates, ferrites, Belite and some CaO remain as uncombined CaO in the material that enters the kiln, this uncombined CaO further reacts, as the material passes through the kiln to form clinker of desired phase composition with at desired levels of free lime. If this uncombined CaO is less, the resultant clinker would have lower free CaO.
Due to fluctuations of moisture in the SAFR feed, the calciner outlet temperature tends to decrease/fluctuate although the calcination is complete, some of the above post calcination reactions of the CaO are decreased, as a result the uncombined CaO is higher, in the material entering the kiln. The reactions in the kiln are affected for the same throughput and either the clinker free lime is high or the clinker shows lesser C3S percentage (depending on the burnability of the kiln feed).
In plants equipped with XRD it would be possible to monitor the uncombined CaO in Hot meal and optimise the Calciner outlet temperatures so as to achieve the desired uncombined percentage of lime as explained above. If the value is much lower than the desired level it would indicate subsequent lower LSF in the clinker, so addition of lime sludge or limestone powder as explained above would maintain the desired clinker specs. These actions, if affected during the day, would help maintain the day’s average clinker quality.
Besides the variability of the moisture percentage, the ash percentage and its composition in SAFR could change the composition of calcining material and finally depending on these changes, the post calcination reactions would be affected, depending on the uncombined percentage of lime value (monitored by XRD of hot meal), the corrections as explained above would help correct the composition and maintain the burning zone performance and the resultant clinker quality. Thus, if the calciner outlet temperature / kiln inlet material / C6 material temp. (as the case may be) is maintained higher and necessary corrections are made through SAFR or through the kiln feed. We can maintain the uncombined CaO at desired level where we could get good kiln performance as well as a good/improved clinker quality even at a higher percentage of AFR/TSR.
In many plants there is a tendency to increase the clinker Fe2O3 as and when there is an excessive dust generation and dusty kiln performance, this attempt to increase Clinker Fe2O3 would not actually help in improving the kiln conditions and maintaining clinker quality. In another plant equipped with XRD, the limestone had higher Fe2O3 content and to compensate for the effect of the varying moisture of SAFR the Calciner outlet temperature was maintained at around 920oC so that the desired post calcination reactions could be achieved and the uncombined CaO (monitored by XRD of hot meal) was maintained at desired levels.
The clinker LSF also could be maintained but the Free CaO tended to be high. The hot meal XRD indicated that the belite formations were lower in hot meal as and when the clinker free lime was high. Although the Silica was contributed from the Solid AFR as this silica was sand/silt, which did not react, the clinker IR also was observed to increase by around 0.4 per cent use of pondash (having reactive silica) along with the solid AFR up to 1 per cent was observed to increase the Belite content of hot meal and the resultant clinker had desired phase formations with lower free lime. For calculation of PSF/Potential phase composition a correction was given to the clinker silica contents (by subtracting the change in IR of clinker).
Thus, it needs to be noted here that in RDF/MSW, SAFR the ash content may have coarse sand grains, which cannot at the calcination stage and it the burnability is sensitive to silica contents, such corrections of use of wet fly ash with the SAFR could be advantageous to maintain clinker quality. However, these corrections have to be affected during the day through XRD monitoring of Hot meal and subsequent Clinker (say after 40 minutes) so that at the end of the day the clinker is of desired quality specs.
Thus, in plants coprocessing higher levels of AFR it is recommended to have a ‘bi-hourly dashboard’ and the day average clinker consistency in Quality Monitored by ‘compliance percentage to clinker specs’ as shown in Tables 1 and 2.
Such a dashboard helps having the entire plant operations involved in taking bi hourly actions so as to maintain the quality and process targets with increase in SAFR/LQAFR thus, achieving a higher compliance percentage to clinker quality specs. This has enabled not only to maintain clinker quality but it also showed improvements in clinker quality.

Actions: In plant with high TSR percentage without XRD
The hot meal samples at different kiln inlet material temperatures were collected at 870,900n and 930oC along with corresponding clinker samples (after say 40 minutes) and the XRD analysis was carried out at external labs. Through the bi-hourly dashboard actions the clinker compositions were maintained as per desired target. The XRD Mineralogy of Hot Meal and clinker XRD are tabulated in Table 3.
Although the plant maintains 95 per cent DOC, the XRD however indicates >99.5 per cent calcination. Thus, even in the absence of XRD using the bi-hourly dashboard optimisation of clinker quality can be made possible, however having an XRD (even a low watts XRD) would always be advantageous, especially if the kiln feed shows moderate burnability.

Other important considerations

  • As discussed above bi-hourly corrections made to clinker composition could be through the SAFR/RDF mix, in one plant it could be use of waste lime sludge/ in another plant use of wet pond ash/ in another use of limestone crusher dust/ high grade limestone powder depending on the corrections desired.
  • In case such materials are not available in the plant for corrections, the necessary actions bi-hourly, to adjust the clinker LSF, could be by changes in proportion of high ash coal + coal Petcoke mix in calciner or it could be even be targeting an appropriate kiln deed composition to accommodate the ash percentage of SAFR/RDF or bihourly changing the feed rate (TPH) of SAFR, as per the bi-hourly clinker composition requirements.
  • Reducing conditions can have substantial effects on clinker quality like problems with sulfur integration, Alite decomposition (strength reduction), conversion from C4AF to C3A (acceleration of setting), change in color of cement (from greenish grey to brownish), the detection of reducing conditions could be done using ‘Magotteaux Test’, it is important to assess the reducing conditions whether internal or peripheral, would indicate possible reasons.
  • Internal reducing conditions indicate that due to changes in liquid viscosity the larger clinker nodules are black from outside but yellow to brownish in the internal core. Such clinker nodules roll down from the transition zone with an unburnt core which disintegrates on cooling due to gamma C2S. Such nodules have high free lime, delocalised or peripheral reducing conditions due to larger size of solid AFR component (shredded size) showing CO peaks.
  • The Hot meal (2Cl+SO3) needs to be reliably monitored using XRF standards of Hot Meal. Every plant would have a threshold value of (2Cl+SO3), value >3.5 is reported to cause severe depositions at kiln inlet/riser duct/cyclones.
  • The kiln system should be able to handle the higher gas volumes (calciner , inlet and preheater).
    Increased percentage of AFR /TSR is associated with increase in limestone pile LSF which is linked to life of mines (Fig:2). This increase in limestone pile LSF would be more plant specific.
  • To lessen the impact on limestone Pile LSF/Mines life the plant would have to use, sweetener limestone (availability/cost), reduce the percentage use of high silica correctives with purer correctives, use petcoke or low ash coal (imported), use of waste lime sludges available from chemical industries.
  • As discussed earlier the plant could use a mix fuel (petcoke + high ash coal), or (mix of petcoke + high ash wastes like Dolochar/spent carbon etc.) in the calciner, the mix ratio could be changed so as to improve clinker LSF during the day (as a bi-hourly actions).
    High ash (high iron/high silica) wastes should not be fired through the kiln fuel; these wastes should be put through calciner fuel if feasible or along with solid wastes. It is always beneficial to have low ash coal (fuel) / petcoke in kilns.
  • It is recommended to use 4 per cent to 5 per cent high LSF Limestone in petcoke grinding (especially for kiln fuel). It improves the efficiency of petcoke grinding and would help to bind the sulphur during combustion in kiln, thus decreasing the SO3 of the hot meal. Using limestone decreases the SO3 fluctuations in the clinker and the excess of CaCO3 forms C3S clusters in the clinker, thus, improving clinker grindability.
  • Petcoke grinding is usually controlled at 1 per cent to 2 per cent on 90 microns. However in certain grinding systems, the 45 microns residue is observed to be as high as 26 per cent to 28 per cent which could create reducing conditions and initiate some coating formation in pre pre-transition zone in kilns.
  • Large storage yards to stock different types of solid AFR would help to mix the waste in certain proportions so as to achieve relative consistency in ash percentage or even chloride contents.
  • An auto-sampler with shredder on the solid AFR conveyor would be useful. However, the analysis time would be around 4 to 5 hours which is too high.
  • If the plant is reaching >25 per cent TSR, from a futuristics angle, having an online Cross Belt analyser like ‘Spectra Flow’ could help analyse moisture percentage, ash percentage and its constituents in real time, enabling rapid corrections to clinker compositions with necessary modifications to the kiln system even much higher TSR levels could be achievable.
  • Higher TSR levels invariably are associated with increase in Hot meal alkalis, chlorides and sulphates and would necessitate chloride bypass.
  • The procurement has a high responsibility of providing appropriate SAFR/RDF fuel of different ash percentage and of different chloride percentage (screened to remove sand/mud/stones).
  • Wastes having CaO rich ash would always be advantageous for the same TPH of solid AFR, the TSR percentage would be higher if the NCY of the sold AFR is higher.

Conclusion
The paper indicates and discusses in some details the avenues for increased TSR percentage without affecting clinker quality. However, depending on calciner retention time and air volume availability there would be a certain maximum TSR percentage that can be achieved. It may be noted here that the kiln system would necessitate suitable upgradation for achieving a much higher TSR percentage. It is needless to mention that XRF Models with standardless software for elemental analysis of solid/liquid AFR would be advantageous and as discussed having an XRD would be a necessity to maintain clinker quality at higher TSR percentage.
Clinkers with High MgO (>4.5 per cent) would be a challenge and optimising the CaO/SiO2 ratio would be a key to improve clinker quality use of XRD in such clinkers would be an asset.
Futuristically, ‘Torrefaction Process’ (the process of degrading organic materials in a nitrogen or inert environment within a temperature range of 200oC to 300oC) of bio wastes if extended suitably to MSW wastes and other solid AFR to produce a bio coal, could become an excellent opportunity for increased TSR for cement plants.
In this paper I have tried to share some observations in a generalised manner made at different plants with different AFR/TSR percentage which could be useful for other plants for their future road map on maximising TSR percentage.

About the author:
Shreesh Khadilkar, Consultant and Advisor brings over 37 years of experience in cement manufacturing, having held leadership roles in R&D and product development at ACC Ltd. With deep expertise in innovative cement concepts, he is dedicated to sharing his knowledge and improving the performance of cement plants globally.

Concrete

30-Day Traffic Diversion In Place For CC Road Works In Madhapur

Diversions in place from May 16 for cement concrete road works

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The Cyberabad Traffic Police issued a traffic advisory as road works begin for the laying of a cement concrete (CC) road from Jaya Shankar Statue to RRR Restaurant at Parvathnagar in Madhapur limits. The advisory indicated that traffic diversions will be in place for 30 days from May 16 to ensure the smooth flow of vehicles and to minimise congestion on the affected stretch. The measure aims to balance uninterrupted construction activity with the movement needs of commuters.

Traffic moving from Toddy Compound towards Parvathnagar village will be diverted at Parvathnagar junction towards Sunnam Cheruvu and the 100 feet road. Local motorists and public transport operators have been advised to follow the diversionary route as directed by traffic personnel on duty. Alternate routes and signage have been planned to mitigate delays and to manage peak hour congestion.

Police officials said the diversion had been planned to facilitate uninterrupted road works while maintaining traffic movement in the area. Commuters were urged to plan their travel accordingly and to cooperate with traffic staff managing the stretch. Authorities indicated that enforcement of diversions would be active and that violations could attract penalties.

The 30 day schedule is intended to allow contractors to complete the laying and curing phases with minimal interruption to vehicular flow. Residents and businesses in adjacent localities have been advised to factor the diversion into deliveries and travel plans. The traffic police promised continuous monitoring of the works and the operational diversions and emphasised that temporary inconvenience was necessary for longer term improvement of the road network. Traffic personnel will be stationed at key junctions and additional signage and temporary markings will be displayed to guide motorists and pedestrians through the revised alignments while public transport services will follow the diversion where feasible and operators have been asked to adjust timetables to minimise disruption.

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Concrete

HeidelbergCement India Receives Consent For Khandwa Grinding Unit

Consent granted by Madhya Pradesh Pollution Control Board

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HeidelbergCement India (HeidelbergCement India) has received regulatory consent to establish a cement blending and grinding unit at Village Dongaliya, Tehsil Punasa, District Khandwa in Madhya Pradesh. The consent was granted by the Madhya Pradesh Pollution Control Board under the Water (Prevention & Control of Pollution) Act, 1974 and the Air (Prevention & Control of Pollution) Act, 1981 and is dated 17 May 2026. The company disclosed the development in a filing made under Regulation 30 of the SEBI (Listing Obligations and Disclosure Requirements) Regulations, 2015.

The project plan envisages procurement of long term availability of fly ash and the allotment of land on lease for setting up the unit. The proposed facility is described as a blending and grinding installation which will process cementitious materials sourced from nearby operations and suppliers. Company filings state the measures required to secure raw material logistics and statutory compliance before commencing construction.

The addition of a grinding unit in Khandwa is intended to strengthen regional supply and improve logistical efficiency by reducing haulage distances for finished product. The unit is expected to complement existing capacities in central India and to offer flexibility in product mix through blending operations. The reliance on fly ash as a supplementary cementitious material will necessitate long term supply agreements with thermal power producers and coordination with waste utilisation policies.

The disclosure to the regulator and to the stock exchanges follows standard corporate governance practice and aims to keep investors apprised of capital expenditure initiatives. The company indicated that subsequent permits and clearances would be sought in accordance with applicable environmental and land use rules. The project is presented as part of HeidelbergCement India’s broader strategy to optimise capacity distribution and to respond to regional demand dynamics.

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PROMECON introduces infrared-based tertiary air measurement system for cement kilns

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The new solution promisescontinuous, real-time tertiary air flow measurement in cement plant operations.

PROMECON GmbH has launched the McON IR Compact, an infrared-based measuring system designed to deliver continuous, real-time tertiary air flow measurement in cement plant operations. The system addresses the longstanding process control challenge of accurate tertiary air monitoring under extreme kiln conditions. It uses patented infrared time-of-flight measurement technology that operates without calibration or maintenance intervention.

Precise tertiary air measurement is a critical requirement for stable rotary kiln operation. The McON IR Compact is engineered to function reliably at temperatures up to 1,200°C and in the presence of abrasive clinker dust. Its vector-based digital measurement architecture ensures that readings remain unaffected by swirl, dust deposits or drift. Due to these conditions conventional measurement systems in pyroprocess environments are often compromised.

The system is fully non-intrusive and requires no K-factors, recalibration or periodic readjustment, enabling years of uninterrupted operation. This design directly supports plant availability and reduces the maintenance overhead typically associated with process instrumentation in high-temperature zones.

PROMECON has deployed the McON IR Compact at multiple cement facilities, including Warta Cement in Poland. Plant operators report that the system has aided in identifying blockages, optimising purging cycles for gas burners, and supplying accurate flow data for AI-based process optimisation programmes. The practical outcomes include more stable kiln operation, improved process control, and earlier detection of process disturbances.

On the energy side, real-time tertiary air data enables reduction in induced draft fan load and helps flatten process oscillations across the pyroprocess. This translates to lower fuel and energy consumption, fewer unplanned shutdowns, and a measurable reduction in NOx peaks. This directly reflects on the downstream cost implications for plants operating SCR or SNCR systems for emissions compliance.

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